I copied my most recent logs here:
https://drive.google.com/drive/folde...uU?usp=sharing
I have been slowly picking away at this and was using MLV to verify that all sensors are working properly, corrections are being applied as expected, and to see how far off my base map is (at least as much as one can tell with a NB sensor). I would say that all sensors appear to be behaving as expected, and that my bike is much happier running a little richer than 14.7:1 at cruising.
I had planned to get ECMSpy Mono installed when I got to the point of needing to modify the tune, so it sounds like I am at that point now!